SeaNews Türkiye - Maritime Intelligence
    Marine-Accidents-SeaNews

    Report: Poor visibility, pilot error caused Hudson River barge grounding

    September 1, 2017
    SeaNews
    3,833 views
    Share:
    Report: Poor visibility, pilot error caused Hudson River barge grounding
    Archive Photo

    Report: Poor visibility, pilot error caused Hudson River barge grounding

    Extreme Hudson River fog and a powerful current contributed to the April 4 grounding of a barge carrying 60,000 bbls. of gasoline at Catskill, N.Y., according to a report from the New York State Department of Environmental Conservation police.

    The 458’x72’ double-hull barge "RTC 150", pushed by the "Meredith C. Reinauer", operated by the Reinauer Transportation Companies, were hauling the fuel upriver to Albany, N.Y., when the articulated tug-barge got into trouble and hung up on a stone channel marker just south of the Rip Van Winkle Bridge.

    The ATB was undamaged in the incident, and no fuel spilled. That was a good outcome for the New York maritime industry, as the grounding occured amid debate over proposed new anchorage areas on the Hudson River, an industry supported proposal vigorously opposed by environmental groups and river towns.

    The Coast Guard has paused its consideration of that plan, while it conducts a study to assess safety risks and other issues. Capt. Steven Hardy, 64, told DEC police he was heading north on the river, pushing against the current in almost zero visibility and relying on electronic navigation.

    At around 8:15 a.m., the GPS indicated the ATB was on the easternmost side of the channel, and Hardy attempted to steer west and back to the channel center, according to the DEC report. As he attempted to correct course, the oncoming river current, spurred by outgoing tide, began to push the tug and barge sideways resulting in an overcorrection of course.

    Hardy attempted to compensate and turn back to due north, but this was not sufficient to correct course before the vessel left the western side of the channel and collided with the rocks adjacent to channel marker 121, lying just north of the Catskill Creek outlet. One witness interviewed by DEC police recalled watching the incident from Dutchman’s Landing Park on the river.

    The man saw only the top and side of the Meredith C. Reinauer through dense fog, as it crossed toward the west side of the river and turned north close to shore before grounding.

    Hardy and his crew commenced pumping ballast to lighten the RTC 150.

    Close monitoring of the process through the day by the Coast Guard, Reinaeur and state officers found no sign of spillage or water entering the barge, indicating the outer hull had not been punctured. Additional inspections later at Reinauer’s Staten Island, N.Y., base confirmed the barge was undamaged by the grounding.

    Reinauer had made preparations for lightering the "RTC 150" if necessary, but pumping ballast and the evening tide coming up the Hudson allowed the ATB to refloat around 9:15 p.m. After anchoring for the night, the tug and barge proceeded to the Port of Albany to next day to offload the gasoline cargo. State officials found no violations as a result of the incident, the report concluded.     

    © Copyright SeaNews

    Comments (0)

    Leave a Comment

    Your comment will be reviewed before publishing.

    SeaNews Türkiye - Maritime Intelligence

    The leading source for global maritime news, shipping intelligence, and logistics analysis. Connecting the oceans of information.

    Lojiturk - Kamer Sokak No: 12/1
    Küçüksu Kandilli 34684
    Üsküdar/İstanbul, TÜRKİYE

    Popular

    • Check back soon...

    Newsletter

    Subscribe to our daily briefing and never miss a headline from the maritime world.

    You can unsubscribe at any time. Privacy Policy

    © 2025 SeaNews Turkey. All rights reserved.